nope .its not fixed.....changing fan made it run cooler for about 5 mins...then boiled.the grub screw im taking about is more of a cap head bolt going into motor under right hand side header.he tried to undo it and it snapped off in his hand.now he relly upset.got the drill out and tried to drill it...what he thought was the remains of the screw was actually a muddy crud.he got that sorted.then the fan.he just happened to look to his right and see the word "front"..oops.swaped it easy enough.still boiling.when i was around the other night i squeezed the top radiator hose and it was only about 1/4 full..the engine was hot.now every car ive owned when running the hose is tight and full of coolant when thermostat is open..
the radiator has been recored,new waterpump,new hoses,new thermostat.and its had a rebuild on the engine.....im thinking the head gasket is on upside down blocking the cooling jacket holes..but gus assures me its correct.he now scratching his head.
oh he got the lights working.he did knock off the earth wire.
i told him to grab steves big block 69,and do a donut in it..that should ease the frustation...its now going to adelaide on a trailer tomorrow.gus will make a few trips down there when motor is out and try and sort it...tis funny..motor was rebuilt about 2 yrs ago.and hes had it running at idle for hours over the last 2 yrs.when he starts it,it idles for a good half hr to charge battery and has never overheated.but now it does and motor has vertually no hrs on it, and never been driven.until now on a trader plate and its a kettle.